TranceManDann Posted January 20, 2016 Posted January 20, 2016 So I shelled out for some insurance today and reconnected the battery after what must be 2.5 years. Unbelievably it started first turn of the key which is amazing. Took it round the block for 10 mins and I didn't break down which was a good start But day 1 = problem 1 with these cars, it didn't feel like there was any boost under load, the turbo gauge sat just above 0 and didn't move, from memory (it's been a while) this used to swing about all over the place so apart from the obvious 'your turbo is shagged' is there something simple it could be? It was ok before it went into storage and hasn't moved for 5 and a bit years. Thanks Sent from my iPhone using Tapatalk Quote
Iangreenfield Posted January 20, 2016 Posted January 20, 2016 Check for boost leaks on all the big pipes and check the vac pipe connections on your balace bar. The std gauge isn't much cop anyway. Quote
ted Posted January 20, 2016 Posted January 20, 2016 If you not done anything too her over the 2.5 years Id do a service and check the hoses as Thay may perished Quote
TranceManDann Posted January 20, 2016 Author Posted January 20, 2016 Thanks guys, one thing u will learn about me is I have lots of enthusiasm for these cars but zero ability to fix them but I will have a look later. Thanks again Sent from my iPhone using Tapatalk Quote
TranceManDann Posted January 20, 2016 Author Posted January 20, 2016 Can't see anything obvious, I knew there was a reason I've been flush for the last 6 years I just couldn't put my finger on why [emoji1] Sent from my iPhone using Tapatalk Quote
RichardS Posted January 21, 2016 Posted January 21, 2016 Welcome back mate.....:thumbup: Quote I have something to say............ It's better to burn out than to fade away..... :tt2:
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