Collected the car from PowerZed yesterday. Jim has spent many hours putting all the parts in the first two photos below onto the car and removing as much of the superfluous guff as possible. The car passed its MOT with flying colours and with the emissions well with limits. Jim emailed me after he took her for the MOT and to quote him "it behaved very well during the journey. It is very quick on boost even at wastegate pressure. You will be impressed I am sure" I'm a very happy bunny! The trip back home was very wet so drove with due caution. I will take her out when conditions improve and I have plumbed the Racelogic traction control back into the new engine harness. I'm very grateful to Jim for all he has done in getting the car to this stage of development in my ownership - a very big thank you! Engine out and all the emissions guff, manifolds and old turbos coming off. Compression tests well within specs for a 90K miles engine. Front of the car stripped down, old HKS SMICs, Recircs and pipe work removed. New CHRA's with billet compressors installed into JWT 530BB turbos. MSP exhaust manifolds installed with new engine mounts and modified brackets to clear AshSpec pipework. JWT 530BB turbos mounted. Work in progress - engine back in. RobZ 62mm TB's installed onto modified plenum. AshSpec 2.5" pipework going on and a lot of other new parts. All back in and bolted up with the very clean and discreet OEM+ look I was after with the modifications. Which continues with the new MAFs, GFB Recirculating BOVs and AshSpec 2.5" pipework under the nose panel. Again a very clean look. Finally the man who made it all happen...
By
AndrewG · 12 hours ago 12 hr
Hello guys
I have some results from the emance consult software that i would love to have a opinion on. I´m almost starting the task of 120.000 service with more stock stuff like a "new" ps pump, new axle bearing, etc..
Then now i got a cable and pluged my portable :) lets see what whappened:
Still trying to to find out why when i hit the brakes more agressively to stop on crossroad or something the car shuts down...
ECU: 23710-37P01
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Power Balance Test Summary On 20-07-2010 17:55:00
Coolant Temperature: 178 Deg {F}
Idle Air: 35 %
Cylinder # 1
Cylinder On Stablized For 2 Seconds
Average RPM When Cylinder Stablized... 878 Rpm
Cylinder Off Sampled For 3 Seconds
Average RPM When Cylinder Is Off... 852 Rpm
Average RPM Drop Result... 26 Rpm
Highest RPM Drop... 78 Rpm
Amount Of Data Sampled When Cylinder Off... 192
Cylinder # 2
Cylinder On Stablized For 2 Seconds
Average RPM When Cylinder Stablized... 929 Rpm
Cylinder Off Sampled For 3 Seconds
Average RPM When Cylinder Is Off... 860 Rpm
Average RPM Drop Result... 69 Rpm
Highest RPM Drop... 141 Rpm
Amount Of Data Sampled When Cylinder Off... 192
Cylinder # 3
Cylinder On Stablized For 2 Seconds
Average RPM When Cylinder Stablized... 943 Rpm
Cylinder Off Sampled For 3 Seconds
Average RPM When Cylinder Is Off... 871 Rpm
Average RPM Drop Result... 72 Rpm
Highest RPM Drop... 143 Rpm
Amount Of Data Sampled When Cylinder Off... 192
Cylinder # 4
Cylinder On Stablized For 2 Seconds
Average RPM When Cylinder Stablized... 947 Rpm
Cylinder Off Sampled For 3 Seconds
Average RPM When Cylinder Is Off... 856 Rpm
Average RPM Drop Result... 91 Rpm
Highest RPM Drop... 147 Rpm
Amount Of Data Sampled When Cylinder Off... 192
Cylinder # 5
Cylinder On Stablized For 2 Seconds
Average RPM When Cylinder Stablized... 927 Rpm
Cylinder Off Sampled For 3 Seconds
Average RPM When Cylinder Is Off... 835 Rpm
Average RPM Drop Result... 92 Rpm
Highest RPM Drop... 139 Rpm
Amount Of Data Sampled When Cylinder Off... 192
Cylinder # 6
Cylinder On Stablized For 2 Seconds
Average RPM When Cylinder Stablized... 916 Rpm
Cylinder Off Sampled For 3 Seconds
Average RPM When Cylinder Is Off... 840 Rpm
Average RPM Drop Result... 76 Rpm
Highest RPM Drop... 153 Rpm
Amount Of Data Sampled When Cylinder Off... 192